GALT, CA, USA
N2716H
Ercoupe (Eng & Research Corp.) 415-C
DURING THE TAKEOFF GROUND ROLL ON A 2000 FT PRIVATE RUNWAY, AT THE POINT TO ROTATE, THE PLT APPLIED BACK PRESSURE, HOWEVER, THE AIRCRAFT DID NOT RESPOND. APRX THREE QUARTERS OF THE WAY DOWN THE RWY THE PLT REALIZED THAT THE ACFT WAS NOT LIFTING OFF AND HE REDUCED PWR AND APPLIED BRAKES. THE ACFT DID NOT STOP IN TIME BEFORE COLLIDING WITH A BUILDING AT THE END OF THE RWY. INVESTIGATION OF THE ACFT ENGINE AND CONTROL SYSTEMS REVEALED NO MECHANICAL FAILURES OR MALFUNCTIONS.
Source: NTSB Aviation Accident Database
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