Aviation Accident Summaries

Aviation Accident Summary MKC87LA162

MEADE, KS, USA

Aircraft #1

N900K

MAXFIELD PITTS S-1S

Analysis

SHORTLY AFTER TAKEOFF, WHILE DEPG TO THE SE, THE ENG SEIZED. ALL OF THE SURROUNDING TERRAIN CONSISTED OF PLOWED FIELDS, SO THE PLT TRIED TO GLIDE BACK TO THE ARPT; HOWEVER, HE HAD INSUFFICIENT SPEED & ALT TO GET ALIGNED WITH THE RWY. DRG THE LNDG, THE ACFT TOUCHED DOWN ON THE SHOULDER OF THE RWY & WAS DAMAGED. AN EXAM OF THE ENG REVEALED THE #3 ROD CAP & BOLTS HAD FAILED. THERE WAS EVIDENCE THE ROD-TO-CRANKSHAFT BEARING HAD BEEN ROTATING IN THE ROD & HAD INITIATED THE FAILURE. THE ENG HAD 21 HRS OF FLT TIME SINCE IT HAD BEEN OVERHAULED.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports