MT. PLEASANT, WI, USA
N6468S
CESSNA 150H
THE STU PLT CLIMBED TO 1600 FT MSL AFT TKOF. SHORTLY AFT LEVEL OFF, THE ENGINE STOPPED. HE ATTEMPTED AN AIR START WITHOUT SUCCESS. DURING THE FORCED LNDG THE NOSE WHEEL DUG IN AND THE ACFT NOSED OVER IN THE SOFT SOIL. DURING A POST CRASH INTERVIEW, THE STU PLT STATED THAT HE THOUGHT THE ENGINE FAILURE MAY HAVE BEEN CAUSED BY CARB ICE. HE STATED THAT HE DID A GROUND CHECK FOR CARB HEAT BUT DID NOT ATTEMPT TO DO ANYTHING IN REGARD TO CARB ICE WHILE IN THE AIR.
Source: NTSB Aviation Accident Database
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