HARLINGEN, TX, USA
N8575
MBB 109
THE SET OF FLOATS WHICH ALLOWS A HIGH FUEL FLOW IN THIS CARBURETOR FOR HIGH POWER SETTINGS USED FOR TAKEOFF, CLIMB, ETC., HAD CRACKED AND SWOLLEN TO SUCH AN EXTENT THAT THEY WERE RUBBING AGAINST THE FLOAT CHAMBER WALLS AND FLOAT CHAMBER SHROUD TUBES. THIS INTERFERENCE PREVENTED ADEQUATE FUEL FLOW FOR HIGH POWER OPERATION OF THE ENGINE DURING THE TAKEOFF CLIMB WHICH TERMINATED IN THE ACCIDENT. THERE WERE NO ENTRIES IN THE MAINTENANCE LOGS WHICH INDICATED ANY MAINTENANCE OR INTERNAL EXAMINATION OF THE CARBURETOR SINCE THE AIRCRAFT WAS NEW (1959).
Source: NTSB Aviation Accident Database
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