DEPTFORD, NJ, USA
N319AU
BOEING 737-2B7
DRG TKOF, AS USAIR FLT 224 WAS CLBG THRU 4000', THE ACFT YAWED/ROLLED RGT. SIMULTANEOUSLY, THE CREW NOTICED THE #2 THROTTLE SLAM/LOCK TO THE IDLE PSN & A CONTINUOUS AIRFRAME BUFFET BEGAN. SOON THEREAFTER, THE #2 ENG SEPD FM THE ACFT & THE BUFFET STOPPED. THE ENG IMPACTED IN AN OPEN FLD, 6 MI FM THE ARPT. JUST BFR IT SEPD, A PAX SAW THE AFT END OF THE #2 ENG MOMENTARILY DROOP ABOUT 30 DEG. AFTER ENG SEPN, THE 'B' HYD SYS LOST PRES & THE TE FLAPS WOULD ONLY EXTD 10 DEG. THE ACFT WAS LNDD SAFELY AFTER AN EMERG GEAR EXTN & DIFFERENTIAL BRAKING WAS USED FOR STEERING. AN EXAM REVEALED THE AFT MOUNT CONE BOLT FOR THE #2 ENG HAD FAILED FM FATIGUE THRU THE THREAD RELIEF UNDERCUT RADIUS. FATIGUE CRACKS HAD INITIATED ON DIAMETRICALLY OPPOSITE SIDES OF THE RADIUS. SUBSEQUENTLY, THE FWD MOUNT CONE BOLTS & SECONDARY SUPPORT CABLE FAILED FROM OVERLOAD.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports