HOMESTEAD, FL, USA
N777GH
EASLEY PITTS S2-E
WHILE CLIMBING THROUGH 600 FEET AFTER DEPARTURE, THE FLIGHT EXPERIENCED LOSS OF ENGINE POWER. WHILE RETURNING TO THE AIRPORT ALTITUDE COULD NOT BE MAINTAINED AND THE AIRCRAFT CRASHED SHORT OF THE RUNWAY. POST CRASH INSPECTION REVEALED THE NUMBER 4 CYLINDER HAD FAILED AT THE POINT THE CYLINDER HEAD AND CYLINDER BARREL ARE SCREWED TOGETHER. METALLURGICAL EXAMINATION REVEALED THE FAILURE OCCURRED DUE TO CORROSION AND DIFFUSION OF IRON FROM THE CYLINDER BARREL OVER A 3 INCH AREA AT THE 3RD THREAD. THIS RESULTED IN FATIGUE AND OVERSTRESS FAILURE. CORROSION WAS FOUND TO HAVE INITIATED DUE TO THE PRESENCE OF CHLORINE IN THE THREADED AREA. WHEN THE CYLINDER WAS OVERHAULED IN FEBRUARY 1980, 214 FLIGHT HOURS BEFORE THE FAILURE, TRICHLOROETHLENE VAPOR DEGREASER WAS USED TO CLEAN THE CYLINDER PRIOR TO OVERHAUL. AFTER USE OF THE VAPOR DEGREASER THE CYLINDER WAS NOT HEATED TO REMOVE ANY EXCESS CHEMICAL FROM THE CRACKS OF THE CYLINDER.
Source: NTSB Aviation Accident Database
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