OCALA, FL, USA
N6824V
MOONEY M20C
THE PLT STATED THAT HE PUT THE GEAR HANDLE DOWN, CONTINUED HIS APCH AND LANDED WITHOUT REALIZING THE GEAR WAS STILL UP. POST CRASH EXAMINATION OF THE LANDING GEAR RETRACT SYSTEM REVEALED THAT THE FUSE FOR THE LANDING GEAR MOTOR HAD BLOWN DURING THE EXTENSION SEQUENCE AND THE GEAR DID NOT COMPLETELY EXTEND AND LOCK.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports