OAKLEY, KS, USA
N2440H
STEVENSON GLASAIR
THE PIC STATED THAT HE HAD NOT VISUALLY CHECKED THE ACFT'S 4 GALLON HEADER TANK PRIOR TO ATTEMPTING TAKEOFF. DURING THE TAKEOFF THE ENG WOULD NOT PRODUCE FULL POWER. THE TAKEOFF WAS ABORTED AND THE PIC INSPECTED THE ENG FOR A MECHANICAL PBLM. AFTER THE INSPECTION A SECOND ATTEMPT TO TAKEOFF WAS MADE. THE TAKEOFF WAS UNSUCCESSFUL AND ENDED IN SUBSTANTIAL DAMAGE TO THE ACFT. A POST-ACCIDENT INSPECTION OF THE ACFT WAS MADE AND IT WAS DISCOVERED THAT NO FUEL WAS PRESENT IN THE HEADER TANK THAT SUPPLIES FUEL TO THE CARBUERTOR. THE PIC STATED HE SHOULD PERFORM A CLOSER PRE-FLIGHT INSPECTION OF HIS ACFT.
Source: NTSB Aviation Accident Database
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