UNALAKLEET, AK, USA
N95248
TAYLORCRAFT BC-12D
THE PRIVATE PILOT WITH 14 HOURS EXPERIENCE IN THIS AIRPLANE DID NOT RECOGNIZE THAT THE CARBURETOR HEAT CONTROL WAS NOT FUNCTIONING PROPERLY. HE DID NOT RECALL DRAINING THE AIRPLANE'S FUEL SUMPS AFTER REFUELING FROM EXPOSED FUEL TANKS PRIOR TO TAKEOFF. CARBURETOR ICE AND PARTICULATE MATTER AND WATER COULD HAVE DEROGATED ENGINE PERFORMANCE. AFTER PWR LOSS DURING INITIAL CLIMB THE PLT WAS UNABLE TO RETURN TO THE ARPT AND LANDED OFF SHORE IN WATER. AFTER RECOVERY THE ENG WA OPERATED. THE DAY OF THE ACC HAD WX COND. FOR CARB ICE.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports