LAKIN, KS, USA
N5654K
BEECH 35-B33
THE ACFT ATTAINED APRX 200 FT OF ALT AFTER TAKEOFF BEFORE THE ENG WAS HEARD CHANGING SOUND BEFORE THE POPPING & BACKFIRING BEGAN, ACCORDING TO WITNESSES. AFTER ALL ENG SOUNDS CEASED THE ACFT DESCENDED RAPIDLY TO A GRASSY AREA OF THE ARPT & LANDED WITH THE LNDG GEAR & FLAPS FULLY RETRACTED. THE ACFT SLID APRX 180 FT FROM INITIAL IMPACT TO A STOP;AFTER ROTATING 180 DEGREES THE ACFT ENDED THE SLIDE FACING IN THE OPPOSITE DIRECTION. POST ACC EXAM REVEALED ALL ENG CONTROLS FULL FWD. THE ENG FUEL SELECTOR WAS ON THE RT TANK. THE ACFT WAS RAISED AND TANKS DRAINED. THE RT FUEL TANK HAD.APRX 1 CUP OF FUEL IN IT. THE LEFT TANK HAD APRX 25 GALLONS. NO BREAKS OR LEAKS IN THE FUEL SYS WERE FOUND. THE FUEL LINES & FUEL CONTROL CONTAINED NO FUEL. THE ACFT WAS LAST SERVICED WITH FUEL ON 4/16/85, THE DAY BEFORE THE ACCIDENT. THE PLT STATED THAT NO FUEL WAS ADDED ON THE 17TH,THE DAY OF THE ACC.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports