COLUSA, CA, USA
N8929Q
Rockwell S-2R
DURING AN AG FLIGHT, THE ENG BEGAN TO SEVERLY BACKFIRE & LOSE POWER. THE PLT ATTEMPTED TO MAKE A FORCED LDG ON THE NEARBY DUSTER AIRSTRIP BUT HAD INSUFFICIENT ALTITUDE TO BE PROPERLY ALIGNED WITH THE RWY. THE ACFT OVERAN THE EDGE OF THE END DISCLOSED THAT ITS #9 CYK EXHAUST VALVE BOSS HAD BROKEN CAUSING VALVE ACTION TO STOP. THE ENG HAD BEEN OPERATED FOR 30 HRS SINCE RECEIVING A MOH.
Source: NTSB Aviation Accident Database
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