JONESBORO, AR, USA
N29WL
BELL OH-13E
THE PLT REPORTED THAT THE ENG QUIT DUE TO FUEL EXHAUSTION. HE ATTEMPTED TO LAND STRAIGHT AHEAD ON SOFT TERRAIN, BUT THE HELICOPTER ROLLED OVER. DURING THE ACCIDENT SEQUENCE, THE MAIN ROTOR BLADES STRUCK THE TAIL BOOM & SCATTERED PARTS AHEAD OF & TO THE RGT OF THE FLT PATH. THE FLAGMAN WAS APRX 100 FT AHEAD OF THE IMPACT POINT & WAS STRUCK BY FLYING DEBRIS. NO FUEL WAS FOUND IN THE FUEL TANK AFTER THE ACCIDENT. AT THE TIME OF THE ACCIDENT, THE PLT DID NOT POSSESS AN FAA HELICOPTER RATING NOR AN AERIAL APPLICATION CERTIFICATE. ALSO, HE REPORTED THAT THE FUEL GAGES WERE NOT RELIABLE.
Source: NTSB Aviation Accident Database
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