DEMING, NM, USA
N5337
GRUMMAN G-164A
THE PLT TOLD FAA HE WAS SPRAYING A COTTON FIELD AND WAS TURNING AROUND FROM A SWATH RUN WHEN THE PROPELLER FEATHERED. THE PLT TOLD NTSB THAT THE ACFT 'PITCHED UPWARD AND LOST POWER.' ACFT TYPE CERTIFICATE SHOWS THAT A HAMILTON STANDARD PROPELLER M/N 2D30/6101A-12-13-14 IS INSTALLED. PROPELLER REMOVED FROM ACFT WAS A HARTZELL M/N HCB3W30-2B, AN UNAPPROVED INSTALLATION. PROP DISASSEMBLY REVEALED A SPACER HAD BEEN PLACED IN RING ASSEMBLY, MAKING IT IMPOSSIBLE FOR PROP TO FEATHER. BLADE CLAMPS INSIDE PROP HUB WEE BROKEN. NO. 1 BLADE WAS IN FEATHERED POSITION, NO. 2 BLADE WAS NEAR FEATHER, AND NO. 3 BLADE WAS PAST FEATHER. THERE WAS NO EVIDENCE OF AN OIL LOSS OR PROP GOVERNOR FAILURE/MALFUNCTION.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports