SHARONVILLE, OH, USA
N51405
CESSNA 150J
ACCORDING TO THE PLT, THE ENG QUIT 4 HRS INTO THE FLT DUE TO 'APPARENT FUEL EXHAUSTION.' HE HAD ENTERED THE BLUE ASH TRAFFIC PATTERN INSTEAD OF GOING TO HIS ORIGINAL DESTINATION BECAUSE HIS FUEL GAGES READ 1/8 FULL INSTEAD OF 1/4 FULL AS HE HAD EXPECTED. THE ENG STOPPED IN THE TRAFFIC PATTERN AT 800 FEET AGL. DURING A FORCED LANDING, THE PLT STALLED THE PLANE INTO THE TREES & IT FELL TO THE GROUND AFTER TREE IMPACT. HE PLANNED HIS FUEL ON DATA IN THE PLT'S HANDBOOK WHICH CALLED FOR AN ENDURANCE TIME OF OVER 5 HRS AT 45% POWER. THE AMBIENT TEMPERATURE WAS 12 DEG ABOVE STANDARD. THE HANDBOOK SAID TO INCREASE FUEL CONSUMPTION 10% FOR EVERY 8 DEG ABOVE STANDARD DAY TEMPERATURE.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports