SAN ANDREAS, CA, USA
N7305V
BELLANCA 17-30
THE PLT TOOK OFF ON A 2 HR FLT WITH ABOUT 6 HRS OF FUEL ON BOARD. ON SEVERAL OCCASIONS DURING THE FLT, HE REPOSITIONED THE FUEL SELECTOR HANDLE. HE STATED THAT WHEN HE MADE A VERY SHALLOW TURN TO THE RIGHT, NEAR HIS DESTINATION, THE ENG SUDDENLY LOST POWER. HE ATTEMPTED TO RESTART THE ENG BY SWITCHING THE FUEL SELECTOR TO VARIOUS POSITIONS, BUT POWER WAS NOT RESTORED. THE PLT ATTEMPTED TO GLIDE TO THE NEAREST ARPT, BUT HAD INSUFFICIENT ALT. SUBSEQUENTLY, HE LANDED THE ACFT IN A FIELD WITH THE GEAR RETRACTED. AN EXAM OF THE ACFT REVEALED NO PREIMPACT PART FAILURE OR MALFUNCTION THAT WOULD HAVE PREVENTED NORMAL OPERATION OF THE ENG. APRX 37 GAL OF FUEL WAS FOUND IN THE FOUR FUEL TANKS. THE LEFT MAIN FUEL TANK WAS FOUND TO BE EMPTY, BUT FUEL WAS FOUND IN THE OTHER TANKS. ONE TANK WAS VIRTUALLY FULL; ONE WAS ABOUT 1/2 FULL; THE OTHER WAS ABOUT 10% FULL.
Source: NTSB Aviation Accident Database
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