VAN NUYS, CA, USA
N9718L
BEECH B19
AFTER DEPARTURE, AT ABOUT 800 FEET, THE RIGHT AIRLERON BECAME DISCONNECTED. THE PILOT WAS ABLE TO MAKE A LEFT TURN, FLY A LEFT HAND TRAFFIC PATTERN AND LAND SUCCESSFULLY. EXAMINATION OF THE AIRCRAFT REVEALED THAT THE RIGHT INBOARD AILERON CONTROL PUSH ROD HAD SHEARED AT THE FORWARD END; THE BEARING HAD SEIZED. A LACK OF LUBRICATION WAS EVIDENT.
Source: NTSB Aviation Accident Database
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