HUNTINGTON BCH, CA, USA
N4840G
CESSNA 172N
THE PLT STATED THAT HE ABORTED HIS FIRST TAKEOFF BECAUSE OF REDUCED ACCELERATION. HE TAXIED BACK, VIA A PARALLEL TAXIWAYAND MADE RUN-ON TYPE TAKEOFF. HE SAID THAT AS THE ACFT CLIMBED TO AN ALT OF APRX 50 TO 60 FT ABOVE THE RWY HE HEARD A THUD AND THE AIRSPEED DROPPED. HE SAID HIS ALT WAS TOO LOW TO ATTEMPT A TURN FOR THE RWY OR FLY OVER A TWO STORY COMMERCIAL BUILDING AHEAD OF HIS POSITION. HE ELECTED TO FLY THE ACFT INTO A LARGE GLASS WINDOW IN THE COMMERCIAL BUILDING. THE ENG OPERATED NORMALLY DURING A POST ACCIDENT TEST RUN. IT WAS NOTED HOWEVER, THE CARB HEAT VALVE COULD NOT BE MOVED TO THE FULL OFF POSITION. WEIGTH & BALANCE CALCULATIONS INDICATE THE ACFT WAS 174 LBS OVER MAX GROSS WEIGHT AT TAKEOFF.
Source: NTSB Aviation Accident Database
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