TAMPA, FL, USA
N401EA
DOUGLAS DC-9-51
WHILE CLIMBING AFTER TAKEOFF THRU ABOUT 3000 FT, THE CREW NOTED THAT THE #2 EPR HAD DROPPED ABOUT .08, FROM APRX 1.82 TO 1.74 EPR. SHORTLY AFTER THAT, THE 1ST OFFICER NOTED THAT THE AVM ON THE #2 ENG WAS AT THE MAX INDICATION. AT ABOUT 4000 FT, THERE WAS A LOUD EXPLOSIVE TYPE NOISE FROM THE REAR OF THE ACFT AS THE RIGHT ENG LOST POWER. THE CREW SECURED THE RIGHT ENG, RETURNED TO TAMPA & LANDED WITHOUT FURTHER INCIDENT. AN EXAM REVEALED THAT TURBINE BLADES HAD EXITED THE SIDE OF THE ENG TAILPIPE. TEARDOWN REVEALED THAT THE HIGH PRESSURE COMPRESSOR CENTER TUBE SEALING RING HAD AN APRX 1 IN (CIRCUMFERENTIAL) PIECE OF HARD SURFACE PLATING MISSING FROM THE OUTSIDE DIAMETER SEALING SURFACE. THIS FAILURE WAS IN AXIAL ALIGNMENT WITH A GAP IN THE REAR PISTON RING. NEITHER RING COMFORMED TO DESIGN SPECS. THERE WAS EVIDENCE THAT HOT AIR CAUSED COKING OF THE OIL. THE TURBINE SHAFT HAD FAILED APRX 13 INCHES FORWARD OF THE 4-1/2 BEARING. THE 4-1/2 BEARING SEALS WERE DAMAGED, 7 DISPLAYED COKE DEPOSITS. THE LOW PRESS TURBINE MOVED AFT INTERMESHING BLADES & STATORS.
Source: NTSB Aviation Accident Database
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