FORT ORD, CA, USA
N5559G
CESSNA 150J
BEFORE TAKING OFF, THE PLT NOTED THAT THE LEFT FUEL GAGE INDICATED A LITTLE LESS THAN 1/2 FULL & THE RIGHT GAGE SHOWED APRX 1/2 FULL. HE STATED THAT A 'VISUAL INSPECTION SHOWED ABOUT THE SAME, AS MUCH AS I COULD SEE.' THE FLT WAS UNEVENTFUL UNTIL THE ENG SUDDENLY LOST PWR ABOUT 3 MILES FROM THE DESTINATION. AN EMERGENCY LANDING WAS MADE ON ROUGH, UNEVEN TERRAIN WHERE THE NOSE GEAR COLLAPSED DURING THE ROLL-OUT. THE PLT REPORTED THAT A FEW MINUTES BEFORE THE POWER LOSS, HE HAD CHECKED THE FUEL GAGES & THEY INDICATED ABOUT 1/4 FULL. AUTOMOTIVE FUEL WAS BEING USED & AN STC HAD BEEN ISSUED FOR THAT PURPOSE. ABOUT 2 1/2 GALS OF FUEL WERE DRAINED FROM THE ACFT.
Source: NTSB Aviation Accident Database
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