BATTLE CREEK, MI, USA
N708ZW
de Havilland DHC-7-102
WHILE CRUISING AT 7000 FT MSL, THE 1ST OFFICER WAS TRIMMING THE RUDDER, USING THE ROTARY SWITCH ON THE CENTER CONSOLE, WHEN HE FELT A 'SNAP' INSIDE THE SWITCH. AFTER THAT, THE SWITCH WOULD ROTATE FREELY BETWEEN THE STOPS. THE ACFT BEGAN YAWING LEFT & RIGHT UNTIL THE CREW PULLED THE APPROPRIATE CIRCUIT BREAKER TO DISABLE THE RUDDER TRIM. SUBSEQUENTLY, THEY LANDED WITH FULL RIGHT RUDDER TRIM. AN EXAM REVEALED THAT A CENTERING SPRING, P/N 42M4231137, WHICH LOADS THE SWITCH TO THE NEUTRAL/OFF POSITION HAD FAILED AT A FATIGUE CRACK.
Source: NTSB Aviation Accident Database
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