SANFORD, FL, USA
N2830V
BEECH 35
THE ENG LOST POWER WHEN THE ACFT WAS ON FINAL APCH TO LAND. THE PLT STATED THAT HE THEN SWITCHED FUEL TANKS, ACTIVATED THE ELECTRIC FUEL BOOST PUMP & WORKED THE RELATED WOBBLE PUMP AS FAST AS HE COULD, BUT WAS UNABLE TO RESTORE ENG POWER. SUBSEQUENTLY, THE ACFT CRASHED INTO A BUILDING AND CARTWHEELED INTO A PARKING LOT. AN EXAM OF THE WRECKAGE REVEALED THE LEFT FUEL TANK WAS EMPTY. ABOUT 10 GAL OF FUEL WAS REMAINING IN THE RIGHT TANK & AN UNDETERMINED AMOUNT OF FUEL WAS IN THE AUX TANK. THE WOBBLE PUMP/FUEL SELECTOR ASSEMBLY'S TANK SELECTOR VALVE, PN 35-924068, WAS MODIFIED, BUT WAS NOT INSTALLED IN ACCORDANCE WITH THE MANUFACTURE'S SPECIFICATION. THE SELECTOR'S DETENT BALL, PN35-921166, WAS MISSING & THE ASSEMBLY'S SPRING WAS RIDING ON THE VALVE. ALSO, THE ASSEMBLY'S HOUSING, PN 35-921185, WAS DAMAGED. IN THIS CONDITION, THE PLT COULD NOT DETERMINE THE EXACT POSITION OF THE SELECTOR VALVE. AN EXAM OF THE ACFT REVEALED IT HAD CRASHED IN A STEEP NOSE DOWN, LEFT WING LOW ATTITUDE.
Source: NTSB Aviation Accident Database
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