PONTIAC, MI, USA
N2GL
FAIRCHILD SA-227-TT
THE AIRCREW NOTICED A 'NOSE UP' PITCH CHANGE DURING DESCENT AT ABOUT THE TIME THEY WERE LEVELING TO SLOW FOR THE ARPT PATTERN & TRAFFIC. THE PLT REPORTED THAT FULL FORWARD YOKE PRESSURE WAS REQUIRED TO STOP THE NOSE UP CONDITION. THE ACFT WAS LANDED WITHOUT FURTHER INCIDENT. AN INVESTIGATION REVEALED THAT THE OCCURRENCE WAS CAUSED BY A WORN HORIZONTAL STABILIZER TRIM ACTUATOR, P/N DL5040M2-4.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports