MADISON, IN, USA
N1187B
LUSCOMBE 8A
THE PILOT STATED AFTER THE ACCIDENT THAT HE PERFORMED A PREFLIGHT INSPECTION OF THE ACFT AND DID AN ENGINE RUN-UP BEFORE TAKEOFF. DURING CLIMBOUT, AT AN ALTITUDE OF 150 FEET THE PLT EXPERIENCED AN ENGINE FAILURE. AN EMERGENCY LANDING WAS MADE IN TREES. THE PLT STATED THAT HE USES A MIXTURE OF 100LL AND AUTOMOTIVE GRADE LOW LEAD FUEL. HE DRAINED APPROXIMATELY 4 GALLONS FROM THE ACFT AFTER THE ACCIDENT. THE PLT DOES NOT HAVE AN STC FOR THE FUEL. NO PREIMPACT PART MALFUNCTION OR FAILURE WAS FOUND.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports