MILLARD, NE, USA
UNREG
AMER. AEROLIGHT EAGLE 2 PLC
THE PLT REPORTED THAT AFTER EXCHANGING THE CANARD ELEVATOR & READJUSTING THE SPOILER CONTROL TELEFLEX CABLE ROD END AT THE SPOILER BELLCRANK, HE TOOK OFF ON A TEST FLT. AFTER ABOUT 5 MIN OF FLT, THE RIGHT SPOILER FAILED TO RETRACT AFTER IT WAS USED DURING A RIGHT TURN. THE PLT TRIED TO MAINTAIN CONTROL BY APPLYING LEFT RUDDER. HE SAID THAT HE COULD STOP THE TURN WITH LEFT RUDDER APPLIED, BUT THIS CONTROL INPUT RESULTED IN THE NOSE OF THE VEHICLE PITCHING UP. WHEN HE REDUCED THE RUDDER, THE VEHICLE WOULD REENTER THE RIGHT TURN & THE NOSE WOULD DROP, PLACING THE VEHICLE IN A SPIRAL. SUBSEQUENTLY, HE CRASH LANDED ON A GOLF COURSE. AN EXAM REVEALED AN OVERLOAD FAILURE OF THE THREADS OF THE TELEFLEX CABLE BELLCRANK. THE REASON FOR THE OVERLOAD WAS NOT VERIFIED.
Source: NTSB Aviation Accident Database
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