AMARILLO, TX, USA
N6283Q
CESSNA 310Q
DURING GEAR RETRACTION ON POST-MAINTENANCE CHECK FLIGHT INITIAL CLIMB, GEAR UNLOCKED LIGHT REMAINED ON AND GEAR EXTEND/RETRACT MOTOR CIRCUIT BREAKER POPPED. PLT RESET CB AND HEARD A 'LOUD POP' FROM THE NOSE SECTION OF THE ACFT. PLT THEN EXTENDED GEAR BUT NOSE GEAR EXTENDED ONLY PARTIALLY. PLT CIRCLED FIELD FOR ABOUT 3 HOURS ,ATTEMPTING UNSUCCESSFULLY TO LOWER NOSE GEAR BY EMERGENCY MEANS. PLT THEN LANDED, SHUTTING DOWN ENGINES AND FEATHERING PROPS BEFORE LOWERING NOSE ON PARTIALLY EXTENDED NOSE GEAR. INVESTIGATION REVEALED THE NOSE GEAR LINKAGE HAD BEEN DISCONNECTED DURING MAINTENANCE AND WAS NOT RECONNECTED.
Source: NTSB Aviation Accident Database
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