CHESTERFIELD, MO, USA
N9373M
MOONEY M20E
THE ACFT CRASHED SHORT OF THE RWY AFTER MAKING A 180 DEG TURN AFTER TAKEOFF FOLLOWING A LOSS OF POWER. THE PLT STATED THAT AFTER TAKEOFF & AT AN INDICATED AIRSPEED OF 100 TO 110 MPH, AT AN ALTITUDE OF 50 FT, THE ACFT ENG STARTED TO LOSE POWER. HE DECIDED TO RETURN TO THE AIRPORT AND THE ACFT STARTED TO STALL WHILE IN THE TURN CRASHING INTOAN OPEN DITCH NEAR THE END OF THE RWY. INVESTIGATION SHOWED A DISCREPANCY OF THE FUEL NOZZLES IN THE NO. 4 CYLINDER WHICH WERE FOUND BLOCKED. THE SERVO FUEL INJECTOR HAD WATER IN THE FUEL CHAMBER & THE FUEL LINE FROM THE FUEL STRAINER TO FUEL CONTROL HAD WASTER MIXED WITH GASOLINE. THE PROPELLER WAS REMOVED & CHECKED NORMAL.
Source: NTSB Aviation Accident Database
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