HOLLAND, MI, USA
N4738G
CESSNA 172N
THE PLT STATED THAT A SLIGHT RUDDER PEDAL MISALIGNMENT CAUSED THE ACFT TO RUN OFF THE RWY & INTO A DITCH DURING THE TAKEOFF ROLL. HE STATED THAT DURING THE FIRST PART OF THE TAKEOFF ROLL THE RUDDER 'DID NOT RESPOND NORMALLY OR AS EXPECTED.' A LATER EXAMINATION REVEALED NOTHING WRONG WITH THE RUDDER PEDAL ALIGNMENT. THE PLT HAD FLOWN ONLY SIX TENTHS OF AN HOUR SOLO FLYING TIME IN THE 90 DAY PRIOR TO THE ACCIDENT.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports