PONTIAC, MI, USA
N9011Y
PIPER PA-31
THE AIRCRAFT DEPARTED THE AIRPORT WITH ONE DRY AIR PUMP INOPERATIVE AND THE OTHER PUMP READING LOW. AIRCRAFT CONTROL WAS LOST DURING AN INSTRUMENT APPROACH IN IMC APPROXIMATELY 2.5 HOURS LATER. BOTH PUMP DRIVESHAFTS WERE FOUND SHEARED IN THE WRECKAGE AND BOTH BROKEN SHAFT SURFACES SHOWED POLISHED SURFACES. DURING FURTHER TESTING IT WAS DISCOVERED THAT TAPE OR PIPE DOPE HAD BEEN USED IN THE THREADING OF THE INTAKE & OUTFLOW FITTINGS OF THE LEFT PUMP. NO CONTAMINANTS WERE FOUND IN THE RT PUMP BUT THE PUMP WALL INNER SURFACES GAP WAS APPRX .005 IN. THIS GAP IS APPROX 50 PERCENT OVER THE ALLOWABLE TOLERANCE FOR A SERVICEABLE AIR PUMP.THE PRESSURE REGULATOR VALVE TO THE ATTITUDE INDICATOR GYRO & THE COMPASS GYRO WERE EXAMINED & FOUND TO REQUIRE PRESSURE EXCEEDING NORMAL REQUIREMENT STANDARDS.
Source: NTSB Aviation Accident Database
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