ANDREWS, TX, USA
N6916L
CESSNA 310K
THE PLT HAD RECEIVED A WX BRIEFING FOR A FLT TO MILAND, TX. A WITNESS REPORTED THAT AFTER TAKING OFF, HE MADE 2 OR 3 TOUCH-AND-GO LANDINGS. DURING TAKEOFF FROM THE LAST TOUCH-AND-GO, WITNESSES OBSERVED THE ACFT PULL UP ABRUPTLY, ENTER A STEEP RIGHT BANK, THEN CRASH & BURN. AN EXAM OF THE CRASH SITE REVEALED THAT THE ACFT IMPACTED IN A NEAR VERTICAL NOSE DOWN ATTITUDE. BOTH PROP BLADES HAD EVIDENCE OF HIGH ROTATIONAL DAMAGE. THE ELEVATOR TRIM TAB WAS FOUND DEFECTED 15 DEG DOWNWARD (NOSE UP TRIM). THE ELEVATOR TRIM ACTUATOR WAS FOUND EXTENDED 1.1 INCHES. NO PREIMPACT PART FAILURE OR MALFUNCTION WAS FOUND.
Source: NTSB Aviation Accident Database
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