GOSHEN, CA, USA
N51763
ENSTROM 280C
ABOUT 5 MIN AFTER TAKING OFF, THE PLT NOTICED A SUDDEN LOSS OF POWER TO THE TAIL ROTOR. HE MADE AN EMERGENCY LANDING IN AN ALFALFA FIELD. HE REPORTED THAT DURING AN AUTOROTATIVE LANDING, HE HAD INSUFFICIENT COLLECTIVE TO FLARE PROPERLY. SUBSEQUENTLY, THE MAIN ROTOR BLADES SEVERED THE TAIL BOOM, AN EXAM REVEALED THAT THE TAIL ROTOR AFT DRIVE COUPLING, PN 28-13609, HAD FAILED. ALL OF THE INTERNAL GEAR TEETH ON THE FEMALE PORTION OF THE COUPLING WERE STRIPPED. THERE WAS EVIDENCE OF INADEQUATE LUBRICATION.
Source: NTSB Aviation Accident Database
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