GILDERLAND, NY, USA
N6191K
REPUBLIC RC-3
ON THE DAY BEFORE THE ACCIDENT, AN EMERGENCY LANDING WAS MADE IN A HAY FIELD AFTER THE ENG LOST POWER. AN EXAM OF THE ACFT REVEALED A DEFECTIVE FUEL LINE. THE FUEL LINE WAS REPAIRED. DURING A GROUND RUN-UP, THE ENG PRODUCED FULL POWER & THE MAGNETO CHECK WAS NORMAL. HOWEVER, DURING A TAKEOFF, THE ENG LOST POWER AGAIN AT APRX 40 FT AGL. THE PLT REPORTED THAT WHILE HE WAS IN A LEFT TURN TO AVOID TREES, CONTROL EFFECTIVENESS WAS LOST & HE COULD NOT LEVEL THE WINGS. SUBSEQUENTLY, THE ACFT CRASHED & WAS SUBSTANTIALLY DAMAGED. AN EXAM OF THE ACFT DISCLOSED FOREIGN MATERIAL IN THE INLET ELBOW OF THE GAS STRAINER. THE PLT STATED THAT THE MATERIAL WAS A BALL OF GUMMY RUST. IN A DIAGRAM DEPICTING ITS LOCATION, HE SHOWED THAT IT WAS NEXT TO A DEFECTIVE HOSE CONNECTION.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports