GREENSBORO, NC, USA
N38234
BEECH A36
THE ACFT LOST POWER DURING THE CLIMB TO CRUISE. THE PLT MADE A FORCED LANDING AND COLLIDED WITH TREES. THE FUEL SELECTORWAS ON THE EMPTY LEFT TANK. THE RIGHT TANK CONTAINED 20 GALLONS OF FUEL. THE PLT DID NOT CHECK THE FUEL SELECTOR PRIOR TO TAKEOFF AND DID NOT REFUEL THE ACFT. THE LAST RECORD OF FUELING WAS ON 9/20/83. THERE WAS NO RECORD OF FLTS OR FLT TIME SINCE THAT DATE. AFTER THE POWER LOSS THE PLT RECALLED TURNING ON THE BOOSTER PUMP BUT DOES NOT RECALL CHANGING THEFUEL SELECTOR. AFTER THE ACCIDENT THERE WAS NO FUEL IN THE FUEL LINES BEING USED. THE ENGINE WAS SUCCESSFULLY RUN AFTER THE ACCIDENT.
Source: NTSB Aviation Accident Database
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