COMPTON, CA, USA
N3630H
Ercoupe (Eng & Research Corp.) 415-CD
THE ACFT EXPERIENCED A TOTAL POWER LOSS ON TAKEOFF & WAS DEMOLISHED IN THE IMPACT SEQUENCE & POST CRASH FIRE. ACCORDING TO SEVERAL INTERVIEWEES THE PILOT HAD PERFORMED EXTENSIVE NON-STC'D MODIFICATIONS TO THE ACFT INCLUDING THE FUEL SYSTEM.AN 'AUTOMOTIVE PERFORMANCE COMPUTER' REQUIRING A FUEL FLOW TRANSDUCER WHICH, ACCORDING TO THE MANUFACTURER, WOULD NOT WORK ON A GRAVITY FED SYSTEM. A FUEL PUMP FOUND IN THE WRECKAGE WAS DETERMINED TO BE A FUEL TRANSFER DUMP DESIGNED TO REDUCE THE OUTPUT FLOW TO ZERO AT ITS MAXIMUM OUTPUT LINE PRESSURE OF 4.5 PSI. THE TRANSDUCER WOULD HAVE REDUCED THE FUEL OUTPUT FLOW TO A 'TRICKLE'.
Source: NTSB Aviation Accident Database
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