NEWBURG, MD, USA
N6385G
CESSNA 150K
THE PLT REPORTED THAT DURING TAKEOFF AT APRX 200 FT AGL, THE ENG BEGAN TO SPUTTER & RUN ROUGH. HE ELECTED TO MAKE A 180 DEG TURN IN AN ATTEMPT TO REACH A CLEAR AREA. HOWEVER, THE ACFT STRUCK A TREE & IMPACTED IN A WOODED AREA. REPORTEDLY, THE ACFT HAD BEEN FLOWN APRX 4 HRS SINCE IT WAS REFUELED. AFTER THE ACCIDENT, THE RIGHT FUEL TANK WAS FOUND EMPTY WHILE THE LEFT TANK CONTAINED AN ESTIMATED 3 TO 4 GAL. A SMALL AMOUNT OF CONTAMINATION WAS FOUND IN THE CARBURETOR BOWL. A CHECK OF THE FUEL LINE FILTER INDICATED A PROLONGED BUILD UP OF FINE SILICONE SILT, RUST PARTICLES & DISOLVED MICE DROPPINGS. AN OPERATIONAL CHECK OF THE ENG REVEALED NO DISCREPANCIES. REPORTEDLY, THE PLT/OWNER HAD USED A STICK, NOTCHED IN INCREMENTS, TO DETERMINE THE FUEL LEVEL BEFORE TAKEOFF. HOWEVER, THE ACCURACY OF HIS METHOD WAS NOT DETERMINED.
Source: NTSB Aviation Accident Database
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