TULSA, OK, USA
N677K
BEECH 95-B55
DURING A MISSED APPROACH FROM A PRACTICE ILS APCH, A LOUD NOISE WAS HEARD DURING GEAR RETRACTION. SUBSEQUENT ATTEMPTS TOEXTEND THE GEAR, BOTH NORMALLY & MANUALLY, RESULTED IN THE RIGHT GEAR REMAINING UP & LOCKED WITH THE INBOARD GEAR DOOR SLIGHTLY OPEN. THE PLT LANDED THE ACFT WITH THE RIGHT GEAR RETRACTED, & THE ACFT SWERVED RIGHT INTO A TAXIWAY DIRECTION SIGN. THE RIGHT GEAR WAS FOUND HELD IN THE UP POSITION BY THE GEAR UP LOCK. A SPRING, P/N 35-815115, DESIGNED TO LIFT THE UP LOCK OUT OF POSITION ALLOWING THE GEAR DOWN SEQUENCE TO BEGIN WAS MISSING.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports