REDDING, CA, USA
N3204Q
PIPER PA-28-181
THE PLT REPORTED THAT WHEN HE TRIED TO START THE ACFT, THE STARTER WOULD NOT 'TURN THE ENG.' THINKING THAT THE OIL HAD CONGEALED, HE EXITED THE ACFT & 'PULLED THE PROP.' AT THAT TIME, THE ENG STARTED & THE PLANE BEGAN TO MOVE. THE PLT JUMPED ON THE RIGHT WING & ATTEMPTED TO GET IN THE COCKPIT TO SHUT DOWN THE ENG; HOWEVER, THE ACFT COLLIDED WITH A PIPER PA-23, N200SA BEFORE HE WAS ABLE TO ENTER THE COCKPIT. THE PLT WAS 'KNOCKED OFF' OF THE RIGHT WING & WAS INJURED. AN EXAM REVEALED THAT THE STARTER GEAR WAS EXTENDED, THE RETAINER BUSHING WAS MISSING & CORROSION WAS FOUND ON THE ROTATER SHAFT. ALSO, THE MAGNETO SWITCH WAS FOUND IN THE 'BOTH' POSITION, THE FUEL BOOST PUMP WAS FOUND ON 'HIGH' & THE THROTTLE WAS 3/4 OPEN.
Source: NTSB Aviation Accident Database
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