Aviation Accident Summaries

Aviation Accident Summary FTW02LA174

Fort Worth, TX, USA

Aircraft #1

N6249R

Cessna 150

Analysis

The airplane had just taken off and was climbing out when the engine started to lose rpm. The airplane continued to climb straight for a couple of hundred feet, then the pilot turned the airplane crosswind hoping to make it around the pattern and land. When the aircraft turned downwind it wasn't climbing, prompting the pilot to make a forced landing in a field. The airplane touched down, impacted a berm, bounced, then impacted the terrain a second time before coming to rest in an upright position. An examination by an FAA inspector revealed the mixture control rod was separated from the carburetor.

Factual Information

On June 7, 2002, approximately 1740 central daylight time, a Cessna 150 single-engine airplane, N6249R, was substantially damaged when it impacted terrain during a forced landing following a partial loss of engine power near Forth Worth, Texas. The airplane was registered to and operated by the pilot. The private pilot and his passenger were not injured. Visual meteorological conditions prevailed, and a flight plan was not filed for the 14 Code of Federal Regulations Part 91personal flight. The flight originated from Hicks Airfield Airport, Fort Worth, at 1735. According to the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2), the pilot had just taken off and was climbing out "when the engine started to lose some rpm." The engine continued to make 2,300 to 2,400 rpm and the airplane was climbing. The pilot stated the airplane climbed straight for a couple of hundred feet, then he turned crosswind. He was hoping to "make it around the pattern and land." He then reported "I turned downwind and was not climbing anymore, and there was a pretty good looking field and the rpm was dropping, so I opted to put down in that field." The airplane touched down, impacted a "hidden berm," bounced, then impacted the terrain a second time before coming to rest in an upright position. According to an FAA inspector, who responded to the accident site, the nose gear was folded aft, the engine mount was damaged, and the firewall sustained structural damage. The inspector also reported that the mixture control rod was found separated from the carburetor.

Probable Cause and Findings

the partial loss of engine power due to the mixture control rod separating from the carburetor. A contributing factor was the lack of suitable terrain for the forced landing.

 

Source: NTSB Aviation Accident Database

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