38 SE BARROW, AK, USA
N59572
BELL 212
WHILE EXECUTING A PRECAUTIONARY LANDING AFTER HEARING A SCREECHING SOUND THE PLT LOST DIRECTIONAL CONTROL & THE HELICOPTER LANDED WHILE SPINNING. EXAMINATION REVEALED THAT THE PRIMARY TAIL ROTOR DRIVESHAFT QUILL COUPLING HAD FAILED. THE 204-040-604-5 FEMALE COUPLING HAD EXPERIENCED HIGH TEMPERATURES DURING OPERATION. CADIUM PLATING HAD BEGUN TO MELT ON EXTERIOR SURFACES. VISUAL OVERHEAT INDICATOR STRIPES REQUIRED BY THE COMPONENT REPAIR & OVERHAUL MANUAL WERE NOT PRESENT ON THE FEMALE COUPLING. THE 204-040-603-9 MALE COUPLING HAD EXTENSIVE HEAT & MECHANICAL DAMAGE.
Source: NTSB Aviation Accident Database
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