Aviation Accident Summaries

Aviation Accident Summary ANC82FA056

38 SE BARROW, AK, USA

Aircraft #1

N59572

BELL 212

Analysis

WHILE EXECUTING A PRECAUTIONARY LANDING AFTER HEARING A SCREECHING SOUND THE PLT LOST DIRECTIONAL CONTROL & THE HELICOPTER LANDED WHILE SPINNING. EXAMINATION REVEALED THAT THE PRIMARY TAIL ROTOR DRIVESHAFT QUILL COUPLING HAD FAILED. THE 204-040-604-5 FEMALE COUPLING HAD EXPERIENCED HIGH TEMPERATURES DURING OPERATION. CADIUM PLATING HAD BEGUN TO MELT ON EXTERIOR SURFACES. VISUAL OVERHEAT INDICATOR STRIPES REQUIRED BY THE COMPONENT REPAIR & OVERHAUL MANUAL WERE NOT PRESENT ON THE FEMALE COUPLING. THE 204-040-603-9 MALE COUPLING HAD EXTENSIVE HEAT & MECHANICAL DAMAGE.

 

Source: NTSB Aviation Accident Database

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