CAPE MAY, NJ, USA
N6897B
PIPER PA-18-150
AFTER DEPARTING ON A BANNER TOWING MISSION, THE PILOT EXPERIENCED A SUDDEN POWER LOSS. HE HAD INSUFFICIENT POWER AND ALTITUDE TO RETURN TO THE FIELD AND ELECTED TO DITCH IN A CREEK. AN EXAMINATION OF THE ENGINE REVEALED THAT THE NO.2 EXHAUST VALVE, PN 75068, HAD FAILED. THE ENGINE HAD A TOTAL TIME OF 3775 HRS AND 1366 HRS HAD BEEN ACCUMULATED SINCE A COMPLETE OVERHAUL.
Source: NTSB Aviation Accident Database
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