BAY MINNETTE, AL, USA
N463RF
GRUMMAN G-164
THE PILOT REPORTED THAT DURING TAKEOFF, HE NOTICED EXTREME HEAT IN THE COCKPIT AND THE ENGINE BEGAN TO SURGE, THEN LOSE POWER. HE LANDED ON THE REMAINDER OF THE RUNWAY AND STOPPED AFTER RUNNING OFF THE END. HOWEVER, THE ENGINE WAS ON FIRE AND THE PLANE WAS SUBSEQUENTLY DESTROYED. AN INSPECTION OF THE ENGINE REVEALED THAT THE FUEL HOSE THAT WENT FROM THE FUEL INJECTOR SERVO UNIT TO THE FLOW DIVIDER WAS SEPARATED AT THE SERVO END AND WAS BADLY DAMAGED BY FIRE. THE ENGINE HAD ACCUMULATED 597 HRS FLIGHT TIME SINCE THE LAST OVERHAUL. THE PILOT REPORTED THAT THE FAILED HOSE HAD ACCUMULATED 657 HRS FLIGHT TIME.
Source: NTSB Aviation Accident Database
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