CULPEPPER, VA, USA
N555CE
PIPER PA-24-260
ABOUT 16 MIN AFTER TAKEOFF THE PLT REPORTED TO ARTCC THAT HE HAD LOST THE ARTIFICIAL HORIZON, GYRO & VACUUM PUMP. RADIO & RADAR CONTACT WAS LOST SHORTLY THEREAFTER. EXAMINATION OF THE VACUUM PUMP FAILED TO REVEAL A PRE-IMPACT FAILURE OR MALFUNCTION. THE ACFT WAS EQUIPPED WITH A PIPER ALTIMATIC III AUTOPILOT WHICH PROVIDES A BACK-UP SYSTEM ENTIRELY INDEPENDENT OF BOTH THE DIRECTIONAL GYRO & ATTITUDE GYRO, & THE VACUUM SYSTEM. SHOULD THESE FAIL, BY DISENGAGING THE ROLL & PITCH OF THE AUTOPILOT & PLACING THE TOGGLE SWITCH OF THE "AUTOFLITE" (BACK-UP SYSTEM) TO THE ON POSITION, THE ALL ELECTRIC AUTOFLITE WILL TAKE OVER & CONTROL THE ROLL AXIS OF THE ACFT. THE ACFT WAS ALSO REPORTEDLY EQUIPPED WITH AN ELECTRIC TURN COORDINATOR OR TURN & SLIP INDICATOR.
Source: NTSB Aviation Accident Database
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