MADISON, IN, USA
N8055W
GRUMMAN AA-1C
AFTER TAKEOFF FROM A TOUCH & GO THE ENG LOST POWER. THE #1 CYL UPPER PLUG LEAD NUT HAD BACKED OFF & THE LEAD WAS FOUND RESTING IN THE PLUG. THE #2 & #4 CYL UPPER PLUG LEAD NUTS HAD BACKED OFF & BOTH LEADS WERE NOT IN THE SPARK PLUGS BUT WERE RESTING ON THE CYL. THE #4 CYL LOWER PLUG LEAD HAD BACKED OFF ALLOWING IT TO DROP OUT OF THE PLUG.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports