CHESTERFIELD, MO, USA
N6338T
BEECH B200
UPON ARRIVAL OVER CHICAGO, IL, THE CREW DISCOVERED THAT THE LANDING GEAR WOULD NOT EXTEND. AFTER NUMEROUS UNSUCCESSFUL ATTEMPTS TO LOWER THE GEAR, THE CREW ELECTED TO RETURN TO THEIR HOME BASE AIRPORT AND MAKE A GEAR UP LANDING. THE LANDING WAS SUCCESSFUL AND THERE WERE NO INJURIES. INVESTIGATION REVEALED THAT A LOCKING NUT HAD BACKED OFF A TAPERED PIN AT THE INBOARD UNIVERSAL JOINT IN THE LEFT MAIN GEAR EXTENSION/RETRACTION TORQUE TUBE. THIS ALLOWED THE TAPERED PIN TO BACK OUT, DISCONNECTING THE TORQUE TUBE FROM THE GEAR DRIVE MOTOR. NO EVIDENCE OF FACTORY TORQUE STRIPPING WAS FOUND ON THE NUT.
Source: NTSB Aviation Accident Database
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