Aviation Accident Summaries

Aviation Accident Summary FTW04FA006

Harrison, AR, USA

Aircraft #1

N680WS

Twin Commander Acft. Corp. 680FL

Analysis

The twin-engine airplane was on the base leg to final turn, about 1-1 1/2 miles from the approach end of the runway when the left engine lost power. Instantly after, the right engine lost power and the pilot feathered both engines. The airplane then impacted a 70-foot high tree and collided with the ground about 1,000 feet short of the runway. The 700-hour pilot reported that he activated the electric fuel boost pumps and switched the fuel selectors from the auxiliary fuel tank positions to the main fuel tank positions, about 17 miles from the airport. He recalled that the fuel gauges indicated approximately 70 gallons of fuel in the main tank and about 10-15 gallons of fuel in the auxiliary tanks. The original installed fuel system was configured with a center tank and two outboard tanks. The center tank was composed of five, interconnected rubber cells, having a total capacity of 150 to 159 US gallons. Each outboard fuel tank was composed of two fuel cells with a combined capacity of 33.5 gallons. The total of the two outboard fuel tanks (four cells) was 67 gallons, providing a total usable capacity of 233 gallons. Each engine had its own fuel shutoff switch. Rotating a switch to the RIGHT OUTBOARD or LEFT OUTBOARD position allows fuel from the outboard tanks to flow to the respective engine and shuts off fuel from the center tank. Rotating a fuel shutoff switch to the CENTER position allows fuel to flow from the center tank to the respective engine, and shuts off flow from the respective outboard tank. Rotating the switch to the OFF position shuts off all fuel flow to the respective engine. There was no cross-feed configuration of the switches. Documentation was found in the historical records that indicated extended range fuel system modifications, however, the information was incomplete. After review of all available records and examination of the wreckage, it was determined that the fuel system configuration/capacity of the airplane at the time of the accident was: 156 gallons for the center tank system; 67 gallons for the outboard wing tanks; and a set of auxiliary tanks capable of holding 21 gallons (records of installation unknown). The total usable fuel capacity was estimated at 244 gallons. Cockpit fuel selector positions were: LEFT Fuel Shut Off Valve Selector-LEFT HAND OUTBOARD; LEFT Fuel Boost Pump-OFF; LEFT Engine Primer-OFF; LEFT Ignition Switch-RIGHT; RIGHT Fuel Shut Off Valve Selector-RIGHT HAND OUTBOARD; RIGHT Fuel Boost Pump-ON; RIGHT Engine Primer-OFF; RIGHT Ignition Switch-BOTH. Airframe fuel shutoff valves were found in the following positions (Each valve position corresponded to the cockpit selectors): Right Wing Auxiliary-OPEN; Right Wing Main-CLOSED; Left Wing Auxiliary-OPEN; Left Wing Main-CLOSED. A total of 37.5 gallons of usable fuel was drained from the uncompromised tanks (unknown amount had leaked at the accident site). Excerpts from the " Normal Procedures" section of the flight manual regarding fuel selector positions for take off and landing: "CAUTION; Burn center tank fuel first, when 100 gallons is shown on center tank gauge, switch to outboard tanks. Do not allow engine to be starved of fuel when outboard tanks run dry. Select center tanks at first indication of fuel pressure loss. Fuel boost pumps must be on when switching tanks." The "BEFORE LANDING CHECK" procedures in the aircraft flight manual state that the Fuel Selector Valves must be in the "CENTER TANK" position before the approach. The manufacturer stated that the simultaneous loss of power of both engines was likely a result of the outboard fuel tanks unporting. No mechanical anomalies were found during examination of the engines or airframe, and usable fuel was available in the center tank at the time of the accident.

Factual Information

HISTORY OF FLIGHT On October 8, 2003, approximately 1825 central daylight time, a Twin Commander 680FL, twin-engine airplane, N680WS, registered to War Eagle Aviation LLC., of Wilmington, Delaware, and operated by Community First Bank of Harrison, Arkansas, was destroyed when it impacted terrain following a loss of power to both engines while on final approach to land on runway 18 at Boon County Airport (HRO), near Harrison, Arkansas. The private pilot and a pilot rated passenger sustained serious injuries. Visual meteorological conditions prevailed and a flight plan was not filed for the Title14 Code of Federal Regulations Part 91 personal flight. The cross-country flight originated from the Springdale Municipal Airport (ASG), Springdale, Arkansas at 1745. During an interview conducted by the NTSB investigator-in charge (IIC), the pilot stated that he had flown the airplane from HRO to St. Louis, Missouri, and then flew to ASG to pick up the pilot-rated passenger for the final leg of the flight back to HRO. The pilot and pilot rated passenger stated that during the departure sequence from ASG, both fuel selectors were in the main tank positions. The pilot leveled off at 5,500 feet MSL, turn the electric fuel boost pumps to the "on" position, switched the fuel selectors to auxiliary fuel tank positions, then turned the electric fuel boost pumps to the "off" position. Approximately 10 to 15 minutes later, about 17 miles from the airport, the pilot activated the electric fuel boost pumps and switched the fuel selectors from the auxiliary fuel tank positions to the main fuel tank positions. The pilot recalled that the fuel gauges indicated approximately 70 gallons of fuel in the main tank and about 10-15 gallons of fuel in the auxiliary tanks. The flight continued to the destination airport for approximately 5-7 minutes, entered the pattern, lowered the landing gear, and selected "approach" flaps. Upon completion of the base leg to final turn, approximately 1-1.5 miles from the approach end of runway 18, the airplane yawed to the left and the left engine "quit." The pilot rated passenger stated, "I think it's the left engine," and then the right engine "quit." Both left and right propellers were feathered. The airplane then impacted a 70-foot high tree about 45 feet from ground level, impacted the ground 50 yards from the tree, and came to rest in a ditch approximately 1,000 feet short of Runway 18. Four witnesses who heard and observed the airplane just prior to and during the accident reported the following information to the NTSB IIC: #1: The manager of a fixed base operator (FBO) on the airport stated that he heard a normal radio transmission from N680WS on UNICOM frequency to enter the pattern for runway 18. Next, he heard the downwind radio call and he didn't think that it was the pilot's voice on the radio. Shortly after that he heard another radio call from N680WS, which was, "final for 18." He stated that he recognized that this last transmission was the pilot's voice. #2: A lineman for the FBO first "heard" engines and observed the airplane as it came over the airport from the west. He stated that the airplane looked normal, and then the airplane made a left turn onto downwind, and continued. Next he observed N680WS turn left onto base then final. Once established on final he noticed that both engines had stopped, and then the left wing drooped and the airplane went below the horizon. #3: A person, who was burning leaves 1.5 miles northeast of the approach end of runway 18, stated that he heard the airplane fly over and then heard a "backfire sound coming from it." He "didn't think anything about it because [he heard] planes all the time, and sometimes they cut their power to practice landings." He added that about a minute or two later, he and his girlfriend heard two "crashing" sounds. #4: A person, who was driving a vehicle on Hwy 65 just north of the approach end of runway 18, stated that he saw the airplane on final approach to runway 18. He observed that the right engine was not turning and the propeller was feathered. He drove under the airplane as it crossed over U.S. 65, he stated that he thought "he's not going to make it, he looked too low", the airplane then went behind the tree line and was obscured. When a break in the tree line appeared he saw the airplane hit the ground well short of the runway on the tapered safety area, the airplane bounced up with the left wing down approximately 15-20 degrees. PERSONNAL INFORMATION The pilot's private pilot certificate was issued on June 23, 1975. His seaplane rating was issued on June 7, 2002. His instrument rating was issued on February 3, 2003 and multi-engine rating was issued on April 2, 2003. According to entries in the pilot's logbook and entries in the flight logbook for N680WS, the pilot's total flight time as of his last logbook entry on May 22, 2003, was 624.7 hours. Entries in an additional flight log, showed that the pilot had flown the accident airplane approximately 86 hours since May 22, 2003. Several airmen, who had either flown with or had given the pilot instruction, reported that he was a safe and "meticulous" pilot. AIRCRAFT INFORMATION The 1964 model 680FL Commander was manufactured on May 1, 1964, and its current registration was dated November 15, 2001. The airplane had a "Standard" Airworthiness Certificate Type, and was approved for normal operations. According to entries in the aircraft's maintenance logs, the last annual inspection was completed on May 27, 2003, at 9,362.3 hours of operation. The airplane was equipped with 2 IGSO-540-B1A engines with Hartzell HCB3Z30-2B propellers. According to entries in the engine logs, the left engine, s/n L-593-50, had accumulated 375.3 hours since its last major overhaul completed on November 21, 2001. The right engine, s/n L-2135-50, had accumulated 450.1 hours since its last overhaul completed on March 7, 1993. According to the records, both engines were last inspected on May 27, 2003. Fueling records revealed that the airplane was fueled with 133.7 gallons of 100LL aviation grade fuel at Harrison Jet Center, Harrison Arkansas, prior to the departure. During an interview with the fueling technician from Harrison Jet Center, he stated that he fueled the left auxiliary first, then the pilot took the ladder and checked the oil in both engines, then returned the ladder to the technician, who then fueled the main fuel tank, and the right auxiliary fuel tank. The technician then rechecked the main fuel tank to see if there had been any change in the level of the fuel during the fueling sequence, there was none. The technician stated that the fuel tanks were "filled to the tabs." According to aircraft historical records, the airplane was originally delivered new with a fuel system capacity of 223 usable gallons. The system consisted of the following components: Center tank and sumps with low point drain. Left inboard fuel cell Left inboard aft cell Left electromechanical shut off valve Right electromechanical shut off valve Left outboard tank system has a capacity of 33.5 gallons Left outboard forward fuel cell Left outboard aft fuel cell with low point drain. Left electromechanical shut-off valve Right outboard tank system has a capacity of 33.5 gallons Right outboard forward fuel cell Right outboard aft fuel cell with low point drain. Right electromechanical shut off valve According to the airplane maintenance manual, the original installed fuel system was configured with three tanks; the center tank and two outboard tanks. The center tank is composed of five, interconnected, synthetic rubber cells, having a total capacity of 150 to 159 US gallons. Each outboard fuel tank is composed of two fuel cells with a conbined capacity of 33.5 gallons. The total of the two outboard fuel tanks (four cells) is 67 gallons, providing a total usable capacity of 233 gallons when all three tanks are filled. Fuel from the tanks flows through fuel supply lines to the fuel shutoff valves, fuel straners, and to the fuel injector which delivers the fuel, under pressure, to the supercharger impeller. The fuel shutoff switches, located on the overhead cockpit switch panels, control the flow of fuel to the engines. Each engine engine has its own fuel shutoff switch. Rotating a switch to the RIGHT OUTBOARD or LEFT OUTBOARD position allows fuel from the outboard tanks to flow to the respective engine and shuts off fuel from the center tank. Rotating a fuel shutoff switch to the CENTER position allows fuel to flow from the center tank to the respective engine, and shuts off flow from the respective outboard tank. Rootating the switch to the OFF position shuts off all fuel flow to the respective engine. There is no cross-feed configuration of the switches. A review of the airplane's available historical records revealed that several fuel system modifications had been installed. The earliest reference to an increased fuel capacity installation appeared on a copy of a Canadian Weight and Balance Statement, dated December 20, 1981which showed and fuel capacity of 274 US gallons. The next reference to increased fuel capacity modification was in an airframe log dated, May 19, 1995, at an hour meter reading of 19.2 hours. The entry read: "Deactivated RH extended Range Aux fuel bladders and moved fuel filler to factory outboard nacelle bladder tanks. CLH was already deactivated previously by persons unknown. Placarded outboard fillers for 33.5 gallons." No additional documentation could be found regarding the details of these fuel system modifications. On May 7, 2002, at hour meter reading 225.5 all fuel cells, except left inboard aft, which was installed on September 10, 1997, were replaced with new PMA approved Eagle fuel cells. The additional auxiliary tanks increased the total fuel capacity by 21 gallons, thus increasing the total usable fuel capacity from 223 gallons to 244 gallons. An entry in the airframe logbook dated May 7, 2002, stated: "Replaced all fuel cells except LT. INBD. AFT which was replaced 9/10/97. All replacement fuel cells were new manufacture received from Eagle Fuel Cells, Eagle River, Wisc, Cells were installed using all new gaskets, clamps and lacing. Aircraft was fueled to maximum capacity with no leaks noted. Aircraft was flown for 1 hour and proper fuel feed and venting was evident." During the examination of the wreckage, 4 additional auxiliary fuel cells per side were found installed with interconnects to the original system. It was noted that the low point drain for the left and right auxiliary tanks had been disabled and had been placarded. Partial Invoice Summary of fuel cell replacement parts: Work order N041902004 refers to P/N AT60-501 (5630060-501) LH INBD FWD cell. Work order N041902005 refers to P/N AT60-502 (5630060-502) RH INBD FWD cell. Work order N031402005 refers to P/N AT62-507 (5630060-501) LH INBD FWD cell. Work order N032202008 refers to P/N AT61-502 (5630061-502) RH INBD AFT cell. Work order N072401018 refers to P/N AT63-501 (5630063-501) LH OUTBD FWD cell. Work order N081701018 refers to P/N AT63-502 (5630063-502) RH OUTBD FWD cell. WAREHOUSE refers to P/N AT64-501(5630064-501) LH fuel cell. WAREHOUSE refers to P/N AT64-502(5630064-502) RH fuel cell. Work order N042402001 refers to the following part numbers: P/N 64AT-507 (5630064-507) LH OUTBD AFT cell. P/N 64AT-508 (5630064-508) RH OUTBD AFT cell. P/N AT-304-1 (5630304-1) LH FWD INBD AUX cell. P/N AT-304-2 (5630304-1) RH FWD INBD AUX cell. P/N AT-301-1 (5630301-1) LH AFT INBD AUX cell. P/N AT-301-2 (5630301-2) RH AFT INBD AUX cell. P/N AT-296-1 (5630296-1) LH FWD OUTBD AUX cell. P/N AT-296-2 (4530296-2) RH FWD OUTBD AUX cell. P/N AT-302-2 (5630302-2) RH AFT OUTBD AUX cell. According to the manufacturer, the proper PMA part numbers for the LH OUTBD FWD and RH OUTBD FWD cells should have been (5630063-503) and (5630063-504) respectively. The proper PMA part numbers for the LH OUTBD AFT and RH OUTBD AFT cells should have been (5630064-503) and (5630064-504) respectively. Fuel Shut Off Valve Information: Right Wing Auxiliary Part number: AV 16B-1159; serial number D8033-0137 Right Wing Main Part number: AV 16B-1159; serial number D3495-0048 Left Wing Auxiliary Part number: AV 16B-1159 ; serial number D8033-0191 Left Wing Main Part number: AV 16B-1159; serial number K3210-0066 After review of all available records and examination of the wreckage, it was determined that the fuel system configuration/capacity of the airplane at the time of the accident was: 156 gallons for the center tank system; 67 gallons for the outboard wing tanks; and a set of auxiliary tanks capable of holding 21 gallons. The total usable fuel capacity was estimated at 244 gallons. A search of available records did not reveal an FAA 337 field approval for the fuel system modification. Additionally, the aircraft flight manual (AFM) did not include information pertaining to the operation of the fuel system with the installed modification. WRECKAGE AND IMPACT INFORMATION The accident site was located within the airport perimeter on a grassy safety area in front of the approach end of runway 18. Evidence at the site showed that the airplane's left wing impacted a 70-foot high tree located about 1,200 feet north of the end of the runway, and about 150 feet left of the extended runway centerline. Remnants of the left wing were found south of the tree, about 50 feet left of the extended centerline, and 1,000 feet north of the end of the runway. The tree had impact signatures approximately 40 feet up from the base. The first evidence of the airplane's impact with the ground was a ground scar about 1,000 feet north of the runway and 125 feet left of the extended runway centerline. The ground scar was about 8-foot wide and 15-feet long, and corresponded to the width of the fuselage. The main wreckage was found laying on its right side in a 12-foot deep ditch, about 250 feet left of the extended centerline and about 750 feet north of the end of the runway. The nose of the airplane came to rest on a heading of 22 degrees magnetic. Both propellers were found in the full-feathered position, and the main and nose landing gears were extended. The 70-foot high tree was found shattered and showed impact marks about 45 feet up from its base. A seven-foot outboard section of the left wing was found forward and to the right of the tree. The fuselage was found resting on its right side, separated and twisted at midpoint. The entire right wing was bent upward, aft, and 45 degrees clockwise from the fuselage. The main cabin and cockpit were found mostly intact with minimal bending and crushing. Cockpit Documentation Left Panel Instrument lights OFF (Associated) Dimmer STOPPED on full CCW Position (Rheostat switch, full counterclockwise stop) Right side Dimmer STOPPED on full CCW Position Trim Wheels (Elevator and Rudder) Free spinning, or not attached to anything (were visually inspected and found to be in neutral position). Engine Oil and Hydraulic Shut Off Switches OPEN POSITION (Guarded type) Circuit breakers were not tripped. Battery ON (3 positions ON, OFF, EXT. PWR.) Left Generator ON Right Generator ON Cabin Lights OFF Navigation Position Lights OFF Beacon ON Left Landing Gear Light OFF Right Landing Gear Light OFF Cabin Door Lock OFF Windshield Alcohol OFF Cabin Heat OFF Cabin Blower OFF Pitot and Fuel Vent Heat (left side) OFF, (right side) OFF. Radios Switch 1 ON (These 2 switches power two avionics' busses) Radios Switch 2 ON Audio Amplifier ON Inverter Switch 1 (3 position; 1, OFF, 2) Propeller Deicer OFF Strobe Light ON De-Ice Single Cycle OFF ( 3 position; Cyc., OFF, AUTO) Com 1 ON 123.00 Nav 1 ON 112.50 Auto Pilot Button OFF LEFT Fuel Shut Off Valve Selector LEFT HAND OUTBOARD ( 3 positions; LHO, Center, OFF) LEFT Fuel Boost Pump OFF LEFT Engine Primer OFF (Guarded spring loaded switch) LEFT Ignition Switch RIGHT (OFF, R, L, BOTH, START) RIGHT Fuel Shut Off Valve Selector RIGHT HAND OUTBOARD (3 positions; RHO, C

Probable Cause and Findings

The loss of power to both engines due to fuel starvation as a result of the pilot's failure to complete the landing checklist while on final approach. A factor contributing to the accident was the lack of suitable terrain for the forced landing.

 

Source: NTSB Aviation Accident Database

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