Sweetwater, TX, USA
N56318
Piper PA-28-235
During cruise flight, the engine lost power and the airplane impacted the terrain short of the alternate airport. The 123-hour private pilot stated the engine "suddenly stopped producing power." He attempted to restart the engine; however, he was not successful. During the forced landing, "strong surface winds came up," and the airplane impacted the terrain approximately 450 feet short of the runway. The airplane then struck trees, a fence, two poles and came to rest on the runway surface. Examination of the engine revealed the crankshaft bolt and crankshaft dowel pin had fractured and failed. The bolt fracture surfaces displayed signatures consistent with fatigue. At the time of the accident, the engine had accumulated approximately 576 hours since major overhaul.
On November 21, 2003, approximately 0800 central standard time, a Piper PA-28-235 single-engine airplane, N56318, sustained substantial damage during a forced landing following a loss of engine power while in cruise flight near Sweetwater, Texas. The private pilot and his passenger were not injured. The airplane was registered to Master Plumbers LLC, Hobbs, New Mexico, and operated by the pilot. Visual meteorological conditions prevailed, and a flight plan was not filed for the 14 Code of Federal Regulations Part 91 personal flight. The flight departed the Lea County Regional Airport, near Hobbs, New Mexico, at 0610, and was destined for Abilene, Texas. The 123-hour pilot stated that during the flight, approximately 7 to 9 nautical miles west of Avenger Field Airport (SWW), near Sweetwater, the engine "suddenly stopped producing power." The pilot attempted to restart the engine; however, was not successful. During the forced landing to SWW, "strong surface winds came up," and the airplane impacted the terrain approximately 450 feet short of the runway. According to a Federal Aviation Administration (FAA) Inspector who responded to the accident site, after impacting the terrain, the airplane struck trees, a fence, two poles and came to rest on the runway surface. The inspector stated the fuselage was twisted, and the horizontal stabilizer sustained structural damage. At the accident site, the inspector rotated the engine crankshaft by hand and continuity to the accessories and valve train was not established. The airframe and engine were recovered for further examination. On December 10, 2003, under the supervision of an FAA Inspector, the Lycoming O-540-B4B5 engine, serial number L-15593-40, was disassembled for examination. Examination of the engine revealed the crankshaft bolt and crankshaft dowel pin had fractured and failed. The bolt fracture surfaces displayed signatures consistent with fatigue. A review of the engine maintenance records revealed the engine underwent a major overhaul, dated October 21, 1988, at 1,762.15 hours total time. The most recent annual inspection on the engine was completed on May 20, 2003, at a total time of 494.8 hours since major overhaul. At the time of the accident, the engine had accumulated approximately 576 hours since major overhaul. Review of the maintenance records revealed no evidence of any uncorrected maintenance discrepancies.
the loss of engine power due to a failure of the crankshaft bolt. A contributing factor was the lack of suitable terrain for the forced landing.
Source: NTSB Aviation Accident Database
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