Aviation Accident Summaries

Aviation Accident Summary ANC04LA027

Bradenton, FL, USA

Aircraft #1

N5304V

Hiller UH-12B

Analysis

The airline transport pilot was on a solo cross-country helicopter flight as part of a helicopter add-on rating. He reported that he thought that there was enough fuel for about 1.7 hours of flight time, but after only 1.5 hours of flight time, as the flight neared the destination heliport, the engine began to run rough and lose power. He said that he lowered the helicopter's collective and entered an autorotation, and selected an unoccupied playground as an emergency landing site. As the helicopter descended into the playground area, he had to raise the collective to avoid a stand of trees, and the main rotor speed decayed. The helicopter's skids subsequently struck the ground hard, and the helicopter rolled onto its right side. The helicopter sustained structural damage to the fuselage, tail boom, and main rotor drive system. The pilot noted that there were no preaccident mechanical anomalies with the helicopter. An FAA inspector who inspected the helicopter and spoke with the pilot, noted that the helicopter's fuel tank appeared empty, and stated that that the pilot agreed with him.

Factual Information

On February 22, 2004, about 1125 Eastern standard time, a skid equipped Hiller UH-12B helicopter, N5304V, sustained substantial damage during an emergency landing following a loss of engine power in Bradenton, Florida. The helicopter was being operated as a visual flight rules (VFR) cross-country instructional flight under Title 14, CFR Part 91, when the accident occurred. The solo certificated airline transport pilot was not injured. Visual meteorological conditions prevailed, and no flight plan was filed. The flight originated at the Orlando Executive Airport, Orlando, Florida, about 1000, and was en route to the Dove Heliport, Sarasota, Florida. During a telephone conversation with the National Transportation Safety Board investigator-in-charge on February 22, the pilot reported that the purpose of the flight was a solo cross-country flight as part of a helicopter add-on rating. He said that he thought that there was enough fuel for about 1.7 hours of flight time, but after only 1.5 hours of flight time, as the flight neared the destination heliport, the engine began to run rough and lose power. The pilot said that he lowered the helicopter's collective and entered an autorotation, and selected an unoccupied playground as an emergency landing site. He said that as the helicopter descended into the playground area, he had to raise the collective slightly in order to avoid a stand of trees, and the main rotor speed decayed. The helicopter's skids subsequently struck the ground hard, and the helicopter rolled onto its right side, sustaining structural damage to the fuselage, tail boom, and main rotor drive system. The pilot noted that there were no preaccident mechanical anomalies with the helicopter. On February 22, a Federal Aviation Administration (FAA) Airworthiness Inspector from the Tampa Flight Standards District Office (FSDO), traveled to the accident site and inspected the helicopter wreckage prior to recovery. The FAA inspector reported that the helicopter's fuel tank appeared to be empty, and that the accident pilot agreed with him.

Probable Cause and Findings

The pilot's inadequate in-flight planning/decision which resulted in fuel exhaustion. Also causal was the pilot's failure to maintain adequate rotor speed, resulting in a hard landing.

 

Source: NTSB Aviation Accident Database

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