Aviation Accident Summaries

Aviation Accident Summary DFW05CA174

Amarillo, TX, USA

Aircraft #1

N345MC

Learjet 25

Analysis

The 7,300-hour captain was unable to maintain directional control of the twin turbojet airplane while landing on Runway 04 during day VMC conditions with winds from 130 degrees at 17 knots. The 13,502-feet-long, by 300-feet-wide-grooved runway was reported as dry at the time of the mishap. The airplane struck a runway distance marker, and exited the runway to the left during landing roll. The left wingtip tank fuel load was 200-300 pounds heavier than the right wingtip during landing. Examination of the airplane by maintenance personnel did not reveal any discrepancies in the fuel transfer system.

Factual Information

On July 1, 2005, at 1130 central daylight time (CDT), a twin-turbojet Learjet 25 airplane, N345MC, was substantially damaged when it struck a runway distance marker following a loss of directional control while landing at the Rick Husband Amarillo International Airport (AMA), near Amarillo, Texas. The airline transport rated captain, commercial pilot first officer, and 2 passengers were not injured. The airplane was registered to MCOCO Inc., of Houston, Texas, and operated by Air America Jet Charter, of Houston, Texas. Visual meteorological conditions prevailed and an instrument flight rules flight plan was filed for the 14 Code of Federal Regulations Part 91 personal flight. The 466-nautical mile cross country flight originated from the William P. Hobby Airport (HOU) near Houston, Texas, at 1010 CDT. The 7,300-hour captain reported in the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) that approximately 30 miles from the airport he noticed the left wingtip fuel tank was "heavy." He started to transfer fuel, and then stopped the transfer due to being on approach and preparing to land. After being cleared for a visual approach to Runway 04 (13,502 feet long by 300 feet wide grooved concrete runway), the pilot stated that he was able to trim the airplane for "hands off." During the final approach, the pilot noted that the airplane "would not bank to the right without almost full right aileron." The airplane "started raising right wing as full aileron was applied, even with the first officer assisting." At this point, the pilot added that the right wing stopped coming up, but would not go level. The captain further reported that he elected to land rather than add full power and go-around, instead of risking a potential roll situation. The captain added that "alignment to runway was off due to right wing." Subsequently, the airplane exited the left side of the runway striking a runway distance marker. The first officer reported to an Federal Aviation Administration (FAA) inspector that the landing fuel load was as follows: Left Wingtip Tank: 600 pounds Left Wing Tank: 1,100 - 1,300 pounds Fuselage Tank: 400 - 500 pounds Right Wing Tank: 1,000 - 1,200 pounds Right Wing Tip Tank: 300 - 400 pounds Maintenance personnel at a repair facility in San Antonio, Texas, where the airplane was ferried for maintenance, stated that they were not able to find any discrepancies in the fuel transfer system. At 1141, the automated surface observation system at AMA reported wind from 130 degrees at 17 knots, visibility 10 statute miles, few clouds at 7,000 feet, scattered clouds at 12,000 feet, temperature 28 degrees Celsius, dew point 13 degrees Celsius, and an altimeter setting of 30.09 inches of Mercury. The runway was reported as dry during the time of the mishap.

Probable Cause and Findings

The pilot's failure to maintain directional control during the landing roll. A contributing factor was the prevailing crosswind.

 

Source: NTSB Aviation Accident Database

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