Skwentna, AK, USA
N9138M
Cessna U206E
The commercial pilot was conducting a 14 CFR Part 135 on-demand passenger flight to a remote, dirt airstrip at a lodge, when he said the airplane began to sink rapidly on final approach. The pilot said he added power, but the airplane touched down short of the runway, collided with a stump, and came to rest inverted. He said there were no known mechanical anomalies with the airplane prior to the accident, but felt the throttle may not have responded appropriately when he added throttle to arrest the descent rate. After deplaning the passengers, the pilot returned to the airplane and checked the throttle, which appeared to function normally. The airplane received structural damage to the wings and fuselage.
On August 21, 2005, about 1300 Alaska daylight time, a Cessna U206E airplane, N9138M, sustained substantial damage during an in-flight collision with terrain on final approach to a dirt airstrip, about 10 miles north-northwest of Skwentna, Alaska. The airplane was being operated by Alaska Air Taxi LLC, Anchorage, Alaska, as a visual flight rules (VFR) on-demand passenger flight under Title 14, CFR Part 135 when the accident occurred. The commercial certificated pilot and one passenger received minor injuries; the three other passengers were not injured. Visual meteorological conditions prevailed, and company flight following procedures were in effect. The flight departed Lake Hood Strip, Anchorage, about 1210. During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) on August 21, the director of operations for the operator said that the pilot reported that the airplane touched down several hundred feet short of the landing area. He said the area where the airplane touched down had been cleared of trees, but the stumps were still there. He said the pilot told him the airplane hit a stump and nosed over, coming to rest inverted. He said the wings, fuselage, and empennage of the airplane were structurally damaged. During a telephone conversation with the NTSB IIC on August 22, the pilot said he was on short final when the airplane started to sink rapidly. He said he added power, but the airplane touched down short of the runway, and collided with a stump. He said there were no known mechanical anomalies with the airplane prior to the accident. In a written statement to the NTSB dated August 31, the pilot wrote that when he applied the throttle to arrest the descent, he felt that the throttle did not respond appropriately. He said after the passengers deplaned, he returned to the airplane to check the throttle, but it appeared to function normally.
The pilot's misjudged distance/altitude on final approach, which resulted in a noseover following an undershoot and in-flight collision with rough/uneven terrain. A factor associated with the accident was the rough/uneven terrain.
Source: NTSB Aviation Accident Database
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