Aviation Accident Summaries

Aviation Accident Summary MIA06LA002

Destin, FL, USA

Aircraft #1

N9199P

Piper PA-46-350P

Analysis

The pilot reported that the landing seemed normal for a few seconds, and then the airplane started to swerve to the right. He tried to compensate with the application of hard left brake and full left aileron, but the airplane continued swerving to the right and departed the runway. The nose gear collapsed, and the airplane then slid approximately 300 feet on the main landing gear and the underside of the cowling before coming to a stop. Examination of the airplane revealed that the engine mount was fractured at the right nose gear actuator attach foot. Rust was visible on the fracture surface, indicating the crack was pre-existing. The crack was in the area that was the subject of a Piper Service Bulletin. The Service Bulletin required operators to inspect the engine mounts for cracks after every 100 hours of flight time, until the engine mount was replaced with a newer model which incorporated one-piece feet at the nose gear actuator attach points. The engine mount installed in the airplane was the original Piper design configuration (two-piece welded foot design). Review of the airplane's maintenance records indicated that the Service Bulletin had not been complied with at the most recent annual inspection conducted 89.1 flight hours prior to the accident.

Factual Information

On October 3, 2005, about 1205 central daylight time, a Piper PA-46-350P, N9199P, registered to Lookout Leasing Co. and operated by an individual as a Title 14 CFR Part 91 personal flight, veered off the runway during the landing roll at the Destin-Fort Walton Beach Airport, Destin, Florida. The private pilot and the passenger reported no injuries, and the airplane incurred substantial damage. Visual meteorological conditions prevailed at the time and location of the accident, and an instrument flight rules (IFR) flight plan was filed. The flight originated from the Lovell Field Airport, Chattanooga, Tennessee, about 1015. The pilot reported that the flight from Chattanooga to Destin was uneventful, and about 5 miles out from the airport, he canceled the IFR flight plan. He obtained weather information from the airport's automated surface observation system and elected to land on runway 14. The landing seemed normal for a few seconds, and then the airplane started to swerve to the right. The pilot further stated that the airplane pulled harder to the right as it slowed down, and that he tried to compensate with the application of hard left brake and full left aileron, but the airplane continued swerving to the right and departed the runway. The nose gear collapsed before the airplane came to a stop. A witness stated that he watched the airplane during the last portion of its approach and that it appeared to be a normal landing. After touchdown, the airplane began to drift to the right and only traveled a short distance, before the nose wheel struck the grass. The nose wheel immediately collapsed, and the propeller blades struck the ground and stopped. The aircraft then slid approximately 300 feet on the main landing gear and the underside of the cowling before coming to a stop. Examination of the airplane revealed that the firewall was wrinkled. Additionally, the mechanic who performed the examination noted that the engine mount was fractured at the right nose gear actuator attach foot. The mechanic reported that rust was visible on the fracture surface, indicating the crack was pre-existing. Piper Service Bulletin (SB) 1103, Engine Mount Inspection, was issued on April 22, 2002. The SB was updated on January 27, 2003 (1103A) and again on November 25, 2003 (1103B). The SB contained the following information. Purpose: It has been determined that cracks may develop on the engine mount in the area of the nose gear actuator feet. This condition typically occurs when the nose landing gear is subjected to excessive loads, possibly through hard landings, rough field operations, excessive speed turns and/or improper towing of the aircraft. PART I of this SB requires a repetitive inspection of the engine mount. PART II of this SB requires replacement of the engine mount. Compliance Time: PART I Inspection to coincide with the next regularly scheduled maintenance event, and each 100 hours time in service or annual inspection, whichever occurs first, thereafter or until PART II of this SB is accomplished. PART II Replacement if cracks are found during the inspection in PART I, replace cracked engine mount. Note: Compliance with PART II of this SB will relieve the repetitive inspection requirements of PART I of this SB. PART II: Insure the new engine mount (P/N 89137-041) has the one piece feet. The old engine mount has a two piece welded foot. This welded area is where the cracks in the engine mounts have been found. Review of the airplane's maintenance records revealed that during an annual inspection in January 2002, the engine mount was "found cracked at the lower actuator attachment point" and replaced with an overhauled engine mount. The overhauled engine mount had been repaired to the original Piper design configuration (two piece welded foot design) by a certified repair station. The most recent annual inspection was performed on January 14, 2005. As of that date, the airframe had accumulated 3,009.6 hours. The logbook entry for this annual inspection did not indicate compliance with SB 1103B Part I. Review of the checklist used by the facility that performed the annual inspection revealed that it was the 100-hour periodic inspection checklist from the Piper PA-46-310P/350P Maintenance Manual. Under the Engine Group section of the checklist, item 43, "Inspect engine mounts for cracks, corrosion, and loose mounting bolts," was initialed as complete. Under the General section of the checklist, item 2, "All Airworthiness Directives, Service Bulletins, Letters and Instructions complied with," was initialed as complete; however, the portion of this item reading, "Service Bulletins, Letters and Instructions complied with," was crossed out. At the time of the accident, the airplane had accumulated 89.1 hours since the annual inspection.

Probable Cause and Findings

The inadequate design of the engine mount which led to cracking of the mount resulting in a loss of directional control and collapse of the nose landing gear. A contributing factor was the failure of maintenance personnel to comply with a service bulletin to inspect the engine mount for cracks.

 

Source: NTSB Aviation Accident Database

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