Aviation Accident Summaries

Aviation Accident Summary DFW07CA129

Sayre, OK, USA

Aircraft #1

N4673

Grumman G-164A

Analysis

The airline transport pilot departed in a single-engine, low-wing airplane for the purpose of aerial application. He reported that during takeoff, at approximately 100 feet above ground level (AGL), the engine lost partial power. He was unable to maintain altitude, and made a controlled descent into small trees off the end of the runway and then nosed over. An FAA inspector examined the airplane, and reported there was sufficient fuel on board for the flight and both water accumulators were empty. The airplane's last annual inspection was on March 21, 2007. At the time of inspection, the airplane had a total of 7,392 hours. The engine had 7,500 total hours, and 100 hours since it was last inspected. The cause for the partial loss of engine power was not determined.

Factual Information

The radial engine lost power during a full-lenght takeoff from the 5,017-foot long concrete runway. The 9,957-hour airline transport pilot was scheduled to perform a local aerial application flight. The pilot reported that the tailwheel-equipped airplane became airborne about the midfield point of the runway. As the airplane neared the departure end of the runway, while at an altitude of 100 feet agl, "engine roughness began" and the airplane was unable to maintain altitude. The pilot held the best climb airspeed and elected to make a controlled descent into small trees located off the departure end of the runway. The airplane nosed over, and came to rest in the inverted position. There was no fire. An FAA inspector examined the airplane and reported there was sufficient fuel on board for the flight and both water accumulators were empty. The airplane's last annual inspection was performed on March 21, 2007. At the time of inspection, the airplane had accrued a total of 7,392 hours. The 450-horsepower radial engine had accumulated 7,500 total hours and 100 hours since it was last inspected. The pilot calculated that weight of the airplane during takeoff was 4,330 pounds, 169 pounds below takeoff gross weight. He also calculated that the density altitude at the time of the mishap was 4,400 feet. The reason for the partial loss of engine power could not be determined.

Probable Cause and Findings

The partial loss of engine power on takeoff-initial climb for an undetermined reason. A factor associated with the accident was the lack of suitable terrain for a forced landing.

 

Source: NTSB Aviation Accident Database

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